Thread: Frustrated ...
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Old 07-20-2011, 02:21 PM   #103
72TealnWhite
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Location: Detroit, Michigan
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Re: Frustrated ...

Quote:
Originally Posted by SCOTI View Post
You're correct.

To add to this discussion..... The vacuum line was off for the trans modulator & there was a wire shorted because it was not secured properly. This would suggest 'poor' follow-up by the techs that did the work. That being said, I would go through all the basic stuff immediately.

Check all wiring surrounding the engine bay. Make sure the grounds are in place & tight/secured @ the engine block, the chassis, & from the cab.
Verify all vacuum related necessities for the motor have the vacuum they need & that the lines are in good shape. You need to also determine why the vacuum charcoal canister had an open port (Did the sloppy techs leave another line off? Is something else not connected? Did they break something & not correct it??).
Verify you have 13+ volts going to the battery.
Verify you have 12+ volts going to the ignition.

I would do all of this before I drove it around the block again.

thanks alot, did what ya said.. everything checks out.. Thanks all. I really appreciate the help i got here.. OFF FOR A DRIVE

nate
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