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02-07-2016, 10:56 AM | #1 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Red's 68 GMC K15 Update
I found this on Craigslist and bought it in October of 2014. I wanted a project but not a huge one as I don't have the garage space (yet) or time to do a frame off. The truck was recently "restored" by the PO. It was originally a Mississippi truck with a 6 cylinder. SPID is gone so I don't know what else was on the truck originally. It has a crate 350 and what seems to be factory air. The front axel has been switched to discs. I intend for this truck to be a daily driver so reliability and comfort is key. On with the pictures....
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02-07-2016, 11:00 AM | #2 |
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Join Date: Oct 2015
Location: Victoria TX
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Re: Red's 68 GMC K15 Update
After I got it home the real inspection began and I found some interesting issues. Motor mounts were hand fabbed, and the engine crossmember was not installed.
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02-07-2016, 11:01 AM | #3 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Thats better....
Wrong mounts though got the correct ones installed now. Last edited by r8e1d; 02-07-2016 at 11:02 AM. Reason: info |
02-08-2016, 12:29 AM | #4 |
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Join Date: Dec 2009
Location: El Dorado Ca
Posts: 3,374
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Re: Red's 68 GMC K15 Update
great looking truck with alot of upgrades,like that you are making things "right", some people should not try to be welders,that old mount is awful
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02-08-2016, 11:49 AM | #5 |
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Join Date: Oct 2015
Location: Victoria TX
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Re: Red's 68 GMC K15 Update
Indeed Jim, people should stay in their skill set for safety at least. I wish I would have taken pictures of the wiring. It is all replaced now with an AAW Classic Update kit. I need to buy gauges to replace the ones I took out. I leaning towards the Classic instruments G stock kit. Any one know if I can remove the front bezel so I can keep my manual choke?
Red |
02-09-2016, 02:52 AM | #6 |
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Join Date: Oct 2007
Location: Spanaway
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Re: Red's 68 GMC K15 Update
Ye that welding job was kinda scary! Nice truck tho!
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Mike. Swamp Rat build thread : http://67-72chevytrucks.com/vboard/s...d.php?t=595019 72 3/4T 4X4 4" BDS Lift 33" BFG's |
02-10-2016, 10:59 AM | #7 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Thanks Swamp Rat!
Started working on the AC electrical yesterday. Found the AC switch connector when i tore everything out and figured it would need a rewire. Can't tell if it was broken off or got hot. Pulled the wire and found 2 jumpers inserted for the compressor switch and blower motor resistor. Funny thing is both components were there and the compressor switch works, I don't know what the Ohm measurement should be for the resistor though. Red |
03-04-2016, 10:44 AM | #8 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Bought a new A/C harness from AAW and got it installed. Rebuilt the A/C control levers. Put it all back together and tested it. Blower would only work on high and the resistor started smoking, guess I need a new one. In the dismay of disassembly to ensure there wasn't a fire in the box I broke off one of the mounting holes on the heater core box. Hopefully I can find one to replace it otherwise Im going to refiberglass it. Tested all of the lights as well. The headlights are super bright after installing relays for them. New Gauges should be here today. I ordered the Classic Instruments G Stock direct fit kit. I'll post pics when I get them. Helpful hint when installing an AAW Classic update harness. Read the fine print for all of the connectors. Took me about 30 minutes to figure out that the neutral safety switch needs to be connected to itself if you want power to the starter.
Red |
03-04-2016, 04:44 PM | #9 | |
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Re: Red's 68 GMC K15 Update
Quote:
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03-06-2016, 11:54 AM | #10 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Thanks for the compliments Jim.
I got these bad boys installed this morning. Decided to re-wire the AAW harness to fit the Classic Instrument harness. It was only one connector for the CI harness figured it would be easier. One wire that isn't supplied at the AAW harness is a constant 12v for the clock. I put a spare connector in the middle of the 12v batt supply for the radio, worked out pretty good. |
03-22-2016, 02:48 PM | #11 |
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Join Date: Dec 2012
Location: Los Banos CA
Posts: 2,705
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Re: Red's 68 GMC K15 Update
Nice looking!!! now that I don't have to stand on the sealing to see it!
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1956 Chevy Bel Air 2 door 1956 Chevy 210 4 Door 1970 K20 LWB project the Hulk build w/Supercharged 4.8L-ly2/4L60E HULK BUILD 1970 C10 Yellow/White Deluxe LWB w/ 5.3L-LC9/6L80E 1968 K10 LWB Dark green my son calls it "THE HULK Jr"HULK JR *SOLD* GO GO!!! |
03-22-2016, 07:02 PM | #12 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Thanks!
One day I must learn the ways of the force. |
03-22-2016, 11:05 PM | #13 |
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Join Date: Dec 2012
Location: Los Banos CA
Posts: 2,705
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Re: Red's 68 GMC K15 Update
"I shall train you my young apprentice "
Save picture to desktop right click Then select rotate clockwise. Click it twice to rotate 180* Post! "You must search your feelings". Oh. Probably enough Star Wars quotes . Lol.
__________________
1956 Chevy Bel Air 2 door 1956 Chevy 210 4 Door 1970 K20 LWB project the Hulk build w/Supercharged 4.8L-ly2/4L60E HULK BUILD 1970 C10 Yellow/White Deluxe LWB w/ 5.3L-LC9/6L80E 1968 K10 LWB Dark green my son calls it "THE HULK Jr"HULK JR *SOLD* GO GO!!! |
09-16-2016, 07:59 PM | #14 |
Registered User
Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Been a little busy lately but some progress has been made. Got a Boyd tank installed along with the Fitech EFI. I always thought my brakes weren't that good and I figured out that I'm only pulling 11" of vacuum. I've heard of guys running power units this low but apparently mine don't, so I also got a hydroboost unit to install. Waiting for the fittings and hose to get here. In preparation I did some measuring. The hydro unit wants to live in the same place my AC compressor does. If it ain't one thing its another.
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09-18-2016, 04:31 AM | #15 |
user # 2756
Join Date: Jun 2001
Location: Chesapeake, Virginia
Posts: 4,612
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Re: Red's 68 GMC K15 Update
Nice truck. How about some more pics of the fitech? Keep up the good work!
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1970 K25, 8' stepside bed 350/465/205 44 up front, 60 in the rear 4.10s rolling on 33" Dunlop MTs 1986 K5, 350/465/208 Dana 60/14 bolt from a cucv 36" Super Swampers TSL/SX 1983 K20 w/ CUCV axles, 350/700R4/208 sitting on 37" Goodyears 1986 M1031 6.2 diesel, TH400/NP205 locker in the rear and a LS in the front, all stock for now..... 1986 K30, 350/400/205 dana 60 and 14 bolt. I kept the drivetrain. Body/bad and chassis are gone. 1981 K30, 350/465/205 dana 60 and dually 14 bolt. Has a G80, and a flat bed. Going to replace the flat bed. 1985 K20, 350/400/208 10 bolt and SF 14 bolt. I wonder where I can find some 1 tons. Hmmmmm |
10-21-2016, 09:28 AM | #16 |
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Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Got a solution to the location of the AC compressor. Move it! So I did. I think it came out pretty clean. Now to address the wiring nest and clean it up.
Jim do you have any thing specific that you want to see? Last edited by r8e1d; 10-21-2016 at 09:30 AM. Reason: Added |
01-28-2017, 11:47 AM | #17 |
Registered User
Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
So this may have gotten out of hand. My transfer case decided to eat a bearing on the interstate, luckily it was heavy traffic and i was able to creep home in 4 high. I have wanted to update to a six speed trans for a while and decided to go ahead and do it. I ordered a round pattern NP205 and found a L83 and 6L80 local. Now to figure out how to mount my AC compressor and a power steering pump solution.
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01-29-2017, 01:47 PM | #18 |
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Join Date: Jun 2006
Location: Utah
Posts: 1,562
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Re: Red's 68 GMC K15 Update
That is a great looking truck! I'm in!
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02-03-2017, 11:35 PM | #19 |
Registered User
Join Date: Oct 2015
Location: Victoria TX
Posts: 40
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Re: Red's 68 GMC K15 Update
Made some progress this week. Got A LOT of parts ordered. The trans is converted to 4WD with the exception of cutting the shaft down. I'm waiting for the NP205 to get here for a test fit first. Got the Dirty Dingo Crossmember in and mocked up. Surprisingly it fit without switching oil pans. $500 savings BTW. I went with ICT Billet mounts pretty good looking pieces. deleted the Fuel vapor purge solenoid with another piece from ICT. More to come. Oh if someone comes across a set of Gen V LT longtube headers for our trucks please let me know.
Red |
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