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04-09-2004, 12:22 PM | #51 | |
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Quote:
The reason drilling through the whole bolt works better is that it weakens the stress the bolt is placing on the threads inside the hole. The way the bolts are made having a void in the center will literally make the bolt smaller - even by a TINY amount. The problem with this is if the hole doesn't go all the way through. You don't want to end up drilling into the head.
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04-09-2004, 03:04 PM | #52 |
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The problem he has with that is that the bolt is in the block, not the head. So he would have to pull the whole engine to take it to a machine shop.
The whole drilling all of the way through the bolt idea sounds like it would help a lot if you can control how deep you are going. I have never thought of that but will have to try that the next time I break a bolt off. I hope its a long time before I have to use that idea though
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04-09-2004, 05:24 PM | #53 |
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Duh...you're right. Sorry.
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'69 3/4 ton C20 2wd-350ci/TH400 '69 3/4 ton Custom 20 2wd-350ci/4sp Manual '99 2wd 5.7 Chevy Tahoe Seattle, WA. |
04-09-2004, 05:55 PM | #54 | |
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Join Date: Apr 2003
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04-09-2004, 11:52 PM | #55 |
Cause the Chicks DIG IT!!
Join Date: Nov 2003
Location: Beaufort SC
Posts: 509
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You know Jeff I think thats the nicestest gesture i"ve ever had. But it is not necessary anymore thanks anyway. I took the truck on base tonight and tried putting welds on it and then welding a washer and then bolt to the washer. Welds kept on breaking. Finally ended up using a torch and we heated the bolt up real goood then hit it with a blast and the EZ out popped right out. then did the weld with the washer and broke the bolt loose but we couldn't get it out cause there was weld in the threads. Ended up drilling the whole bolt out. I put the old pump on to use as a guide so I wouldn't screw up the hole but sure as heck I did. It went in at a slight angle and I ended up taking out some of the inside of the blind nut. (The bottom bolt for the water pump goes straight into the water jacet but the top bolt hole does not have water to it) It was kinda cockeyed but when I put the pump on it was aligned for it, so I figured I'd just get a tap and try to tap the hole. God was laughing at me again today as I broke the tap inside the hole yet again Tools went flying everywhere as i was a little preterbed. I ended up getting the tap out with a pair of needle nose. Well to sum it all up I bolted up the water pump and fired it up and coolant came spraying out from around that top bolt i had just repaired. Shop was closing and kicked me out so I had to drive the 5 miles home like that as I didn't have the guy with the trailer anymore. Had to stop twice and let it cool down as it pretty much drained all the coolant which is a good thing only as I am draining it tomorrow to put a fricking heli coil in there. Well at least I got a good weekend of getting drunk in front of me if this works tomorrow
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04-10-2004, 01:41 AM | #56 |
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Join Date: Apr 2004
Location: Little Valley, N.Y.
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working in the business of fixing cars and trucks
we get over heating complaints like yours quite often with the heat going up and the heater blowing cold air then everything is ok then it is not usually, i say usually it is a bad head gasket combustion is forced into the cooling system creating an air pocket if you take it to a shop they should be able to test it pretty cheap with a tester that sucks air out of the rad and checks for co and turns the dye blue from yellow the test takes less than 1/2 hour usually good luck
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67 CHEVY LONGBED----- BEST 51 DOLLARS EVER SPENT ON EBAY! 4.3 LITER INJECTED MOTOR WITH 5 SPEED GOING IN SOON |
04-10-2004, 12:36 PM | #57 |
Cause the Chicks DIG IT!!
Join Date: Nov 2003
Location: Beaufort SC
Posts: 509
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Johnny what do you guys do after that test? I was thinking the same thing so I took it to a shop a while back. We got a very few bubbles that started to come up which were ordinary but the mixture stayed yellow. No CO.
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04-10-2004, 05:11 PM | #58 |
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Join Date: Apr 2004
Location: Little Valley, N.Y.
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IM SORRY TO SAY THAT WE HAVENT HAD A FAILURE THAT DIDNT TURN THE DYE BLUE EXCEPT ONE
WE HAD ONE CHRYSLER THAT BARELY CHANGED THE DYE BUT YOU COULD HEAR THE BUBBLES IN THE HEATER CORE AS THE HEAT CAME AND WENT WHEN WE CHANGED THE HEAD GASKETS (BECAUSE WE WERE AT OUT WITS END)WE FOUND A BAD GASKET A TINY SPLIT JUST LUCKY I GUESS WE ALSO HAD A CAR DO THIS BUT IT ENDED UP THAT THE IMPELLER ON THE WATERPUMP HAD ERODED AWAY IT WOULD OVERHEAT WHILE IDLEING BUT I SEE YOU WERE WORKING ON THIS PROBLEM EARLIER WE HAVE ALSO HAD TROUBLE WITH OLD DYE PLACE IT NEAR THE TAIL PIPE AND IT HOULD TURN BLUE THEN GO OUTSIDE AND SIPHON AIR THRU THE TESTER AND THE DYE SHOULD RETURN TO YELLOW IF NOT START WITH FRESH DYE CARQUEST UP HERE IN NY CARRIES IT PRETTY CHEAP WITH THE TESTER ALSO I BELIEVE GOOD LUCK
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67 CHEVY LONGBED----- BEST 51 DOLLARS EVER SPENT ON EBAY! 4.3 LITER INJECTED MOTOR WITH 5 SPEED GOING IN SOON |
04-10-2004, 05:13 PM | #59 |
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ALSO MAKE SURE YOU DONT CONTAMINATE THE TESTER WITH ANTIFREEZE DRAIN ENOUGH OUT WHILE THE TRUCK IS RUNNING AND HOT
THEN USE THE TESTER MAKING SURE YOU DONT SUCK GREEN STUFF IN HOPE THIS HELPS
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67 CHEVY LONGBED----- BEST 51 DOLLARS EVER SPENT ON EBAY! 4.3 LITER INJECTED MOTOR WITH 5 SPEED GOING IN SOON |
04-10-2004, 08:44 PM | #60 |
Cause the Chicks DIG IT!!
Join Date: Nov 2003
Location: Beaufort SC
Posts: 509
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Well to all who have been following my shananigans and giving me advice along the way which I really appreciate by the way I have finally come to the conclusion. the truck is going..............NOTTTTTTTTTTTTTT Bought me a helicoil kit today and some silicone and wish some pushing and cussing and spitting she all went back together and don't leak. I drove the truck around for awhile tonight and it seems alright. Cruising around don't break 210 but when I stopped and Idled and held the foot on the brake it got up to about 230 which isn't great but is not bad for the problems i've been having recently. I'm thinking if I put the shroud back on there and maybe dip my thermostat down to 165 instead of the current 190 I should be alright. Once again thanks to all who contributed and have a great easter weekend
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04-10-2004, 10:05 PM | #61 |
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Good News!! Onward and upward now.
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